Here you can follow the progress of a complete rebuild of my Quickie Q2 with a Revmaster 2100D (65HP) aircraft engine. I severely damaged the aircraft in an off airport (highway) forced landing due to a separated (spliced) mixture cable. Also my VISION aircraft build is at: https://calvinthorne2.blogspot.ca
Q2 Tracker Link
(Cochrane Alberta Canada) Follow recent flights at: https://aprs.fi/cgmbk *******************Also YouTube channel: https://www.youtube.com/channel/UCfxJXIwvmfNlNF3gwplFw7Q
Tuesday, May 17, 2016
Test Flight #2 of Q2 C-GMBK
May 17/16 Springbank Airport elevation 3960 ft using the 5000 foot runway. After much calculating of weight and balance and reading of others who have had the similar problem I decided to test fly again with more weight in the aircraft. My first flight was with 5 gallons of fuel in the header tank which is ahead of the instrument panel and only my personal weight of 160 pounds. This had me nose heavy flying on the forward edge of the "Centre of Gravity" envelope. On this second flight I would have 5 gallons in the header tank and 2 gallons in the main fuselage tank, 58 pounds of sand in the passenger seat, 25 lbs. of lead in the baggage compartment and my weight of 160 pounds. I took off with and initial one circuit to see if all was going well, it was and I climbed to 6000 feet for orbits off to the unused side of the airport. I remained aloft for 55 minutes and found that I could not trim the aircraft for level flight and my pitch trim was always at maximum for nose up attitude. Some constant aft pressure was still required on the stick but much less than previously. I came around an landed a much better landing this time. More calculating is required to identify this problem.
Wednesday, May 11, 2016
Test Flew Quickie Q2 C-GMBK
May 11/16 I test flew the Q2 for one circuit at the Springbank airport west of Calgary. The test flight showed that I had a much to forward C of G or something else was causing the nose down attitude. I could not trim out the aircraft and had to hold lots of aft stick pressure. I kept the circuit high and had 1000 feet on final for good forward speed of 90 on final. A two bounce landing had me rolling out and wondering what was wrong. I had to hold full up elevator in the ground effect and I was probably three feet high causing the bounces before rolling out. Another serious look at aircraft loading is in order.
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